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Appendix B - Details of the Experimental Program
Pages 59-68

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From page 59...
... The prestressing strand was Grade 270 low relaxation. CONNECTION CAPACITY: STUB SPECIMEN TESTS Connection Details The stub specimens consisted of two 16-ft-long AASHTO Type II girders connected by a diaphragm (see Figure B-1)
From page 60...
... The section is treated as a regular reinforced concrete section and uses 0.9 as the understrength factor. For the bent-bar connection, the composite cross section was designed as a regular reinforced concrete section with an ultimate capacity of 1.2 Mcr.
From page 61...
... A load cell placed under the stationary end verified that the loading was correct. The specimen was loaded to simulate a condition where the time dependent and the temperature effects created a positive moment of Mcr, and then traffic loads cycled the moment at the connection above or below Mcr.
From page 62...
... Loading yoke. LOAD CELLS GIRDER VIBRATING WIRE STRAIN GAGE DCDT DIAPHRAGM Figure B-5.
From page 63...
... The positive moment connection was designed as a reinforced concrete section using the composite cross section and the strength of the diaphragm concrete. As with the stub specimens, the connection was designed for a capacity of 1.2 Mcr.
From page 64...
... Figure B-8. Full-size bent bar specimen.
From page 65...
... Location of vibrating wire gages in the full-size specimen diaphragm.
From page 66...
... To generate the cracking moment of 417 k-ft, an internal moment of 278 k-ft was required. This could be achieved with a 1.375-in.-diameter Dywidag bar placed as shown in Figure B-12 and tensioned to the maximum allowable force of 160 k.
From page 67...
... Span 2 was unloaded. The upward loads created positive moment, and downward loads created negative moment.
From page 68...
... Behavior of Untensioned-Bonded Prestressing Strand. Final Report 77-1, Missouri Cooperative Highway Research Program, Missouri State Highway Department, June 1980.


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